Before testing it out, I insulated all of the drain plumbing between the sink, shower and the DWHR pipe. Before...
...and after. The insulating project is to retain the heat and also for sound abatement, since the bathroom is directly above the dining room. For this I used several layers of foam 'sill seal' material wrapped around the pipes and taped.
Here is the vertical transition going into the chaseway:
I noticed most of the water noise was coming from the vertical transitions, so I insulated this area with XPS foam board and copious amounts of spray foam- not pretty, but it really cut down the noise and will contain the heat very well.
Here is the vertical transition going into the chaseway:
I noticed most of the water noise was coming from the vertical transitions, so I insulated this area with XPS foam board and copious amounts of spray foam- not pretty, but it really cut down the noise and will contain the heat very well.
The building's incoming cold supply water (from our well water) always passes through the heat exchange unit on its way to the hot water heater, automatically extracting heat from the warm water running down the drain line. When I installed the DWHR plumbing, I added two gauges for monitoring the water temp going in, and coming out of, the heat exchanger:
Today, I ran hot water through the shower to see how the DWHR would perform- results look good! With the shower running at 101F, the incoming cold well water was being 'preheated' from an initial 50F temp up to about 72F, capturing 44% of the otherwise down-the-drain heat! The manufacturer claims up to 57% efficiency is possible with this model, but that figure is based on a drain water flow rate of 5gpm- much higher than our low-flow sink and shower will ever provide. I'm guessing that around 40% is to be expected and is still very good. And the best part- the DWHR unit was virtually free- our electrical utility provider offered a $400 rebate for installing this $500 system, so the payback should be less than one year. Even at full price, this appears to be a very wise investment and a great energy conservation project. I'd be curious to hear what results others are having with the DWHR units.
Today, I ran hot water through the shower to see how the DWHR would perform- results look good! With the shower running at 101F, the incoming cold well water was being 'preheated' from an initial 50F temp up to about 72F, capturing 44% of the otherwise down-the-drain heat! The manufacturer claims up to 57% efficiency is possible with this model, but that figure is based on a drain water flow rate of 5gpm- much higher than our low-flow sink and shower will ever provide. I'm guessing that around 40% is to be expected and is still very good. And the best part- the DWHR unit was virtually free- our electrical utility provider offered a $400 rebate for installing this $500 system, so the payback should be less than one year. Even at full price, this appears to be a very wise investment and a great energy conservation project. I'd be curious to hear what results others are having with the DWHR units.
Since the bricks were laid with tight joints, I wasn't sure exactly how to go about the grouting process. Having absolutely zero experience with tile work at the time didn't help- so I decided to leave it 'as is' and come back to it later...that was 2008! Finally, almost two years later, I vacuumed all the debris out of the cracks (which amounted to over 3 gallons of sawdust and wood chips), and got started. I mixed some home brew grout using 2.5 parts sand to 1 part Portland cement- then with my mom's help we worked the powder it into the cracks using an experimental sweeping, rubbing and putty knife-packing technique. This worked relatively well, albeit very messy.

I gave the pathway a few more sprayings of water over the next few days, letting the grout set up. Then it required about a dozen moppings to remove the haze of grout that was all over the rough-textured surface (I had put two coats of
The grout was VERY slow to harden using this method, and required some touch up in certain places where there didn't seem to be enough Portland in the mix for it to set. I changed the sand/Portland ratio to 2:1 for the touch up work and this seemed to be much better...more lessons learned on the rocky road of barn-building.
I milled slabs for the stair treads from some maple logs (these were from overgrown trees removed from the city streets in our nearby town).





At the top landing, I built a small linen cabinet. The door pull was made from a hay rake handle that I found on the farm years ago (and saved for something like this).
The stair treads have a variety of nail holes, knots, and worm holes to keep it real.
Final task is to fabricate a curved handrail...I'm still scratching my head over that one.
Normally, the absorber plates are fastened to the plywood backing of the collector framework, sandwiching the copper tubing in between. However, because I wanted a modular design that could be easily disassembled, I opted to build the fin-tube assembly separate from framework. I basically followed
Using a pair of modified Vice Grip 'clamps' (I had a friend weld these up for me, but they can also be purchased from the
Next, the clamps are moved towards the center of the absorber plate and two more sets of screws are placed as shown. I found it beneficial to stand on the clamp with one foot to flatten out the absorber plate as much as possible before attaching the screws.

...and a total of 24 plates per collector.
Once the collector is finished, it could be lifted off the plywood work surface and the foam strips are easily peeled off the tips of the screws from behind. The result looks as follows- great contact between the aluminum and the copper!
The finished assembly is light and easily
Two panels finished, seven more to go!
Once all nine collectors were finished and connected back into the framework, I painted the whole system with
The remainder of the bull work consisted of burying insulated water lines as well as power and communication wires between the solar array and the barn. I rented a Ditch Witch for a day to carve a trench about 150 feet across the yard. I was able to get about 30" deep with this machine- not below the frost line, but since the system will contain anti-freeze, it shouldn't be a problem. When the barn foundation was put in, I included a run of 
The cured insulation assemblies (each 8 feet long) were positioned over the trench and 1"
Once the finished assembly was cured, I turned it on edge (it was too wide to fit in the 5" trench otherwise) and covered the top and sides with poly. The poly was taped around the insulation to hold it in place during installation.
Finally, the wood
I left a couple feet of